Better Half VW Builders Log

 

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 This is a log of the process while building my ½ VW engine. I used a combination of two different sets of plans. Leonard Millholland’s Better Half VW and Scott Casler’s Hummel Engine plans. Most of the parts were bought through Hummel Engine. I was going to try all of the machining myself but decided to buy the major components instead.

 

 I started out by buying a well used VW engine thinking that I could use most or at least some of the parts to save money. After tearing down the engine, I realized that most of it was just a big pile of junk and the only thing that was useable would be the engine case.

 

 

 I took the case down to my local Napa auto parts store and had the case put through their hot soap cleaner. It came out pretty good. There still was some hand cleaning to do but this saved a lot of work.

 

 

 

 

 

 

 

 

 

I made the rear cylinder blank off plates out of 2024T3 aluminum. I first made a cardboard pattern then traced it over to the aluminum and cut it out with my jig saw and finished them off with a hand file.

 

 

 

 

 

 

 

 

 Next was making the cover plate that blocks off the oil cooler line holes. This was done also by making a cardboard pattern and tracing it on to a 3/8 piece of 2024T3 aluminum. This is a little thicker than the plans call for. After talking with Steve Kiblinger, this was needed due to the high oil pressure going through the small area.

 

 

 

 

 

 Next was making the rear cover plate that blocks off where the rear main bearing goes. I spaced the hole for six (6) ¼” coarse thread bolts.

 Instead of making two plates that block off the unused rear push rod holes, I drilled and tapped the holes with a ¾” NPT pipe tap. I used a big drill press in the EAA”s restoration shop for this process. My press was not big enough. It was quite a chore to hold down the case and tap at the same time. I bought four (4) ¾” pipe thread aluminum plugs from McMaster Carr Supply Co. down in Atlanta to seal the holes. After talking with Scott Castler of Hummel Engines, I could have saved a ton of work by using his aluminum plugs that can just be tapped in with a hammer.

 

 

After most of the plates were made it was time to modify the case. The case is a Model “AJ” which is a suitable case for our modification. Turns out to be from 1975.

 

 

 

After bolting the two case halves temporarily together, I held the rear plate that blocks off the rear bearing to the back side of the engine and marked where the six (6) holes will go. Then I unbolted the engine halves and drilled and tapped the holes with a ¼ course thread tap.

 

 The oil passages that lead to the rear of the engine were blocked off by using the rear plugs on the back side of the oil galley. I used a thin brass punch to drive the plugs through the oil galley, then picked them up with a small pair of pliers and tapped them in place between the two lifter bore passages. After this was accomplished I drilled and tapped the rear plug areas that were removed with a 5/16” tap and secured the holes with 5/16 allen set screws.

 

 

 

 

 

 I did one more modification to the case that was recommended by another builder that had a problem with his distributor moving from the timed position he set while in flight. This modification has you drill and tap a set screw on the front side of the case in front of the distributor.

 

 

It’s called a grub screw. The placement of the hole is measured down to where the rubber grommet seal is between the distributor shaft and where the drive gear is. This set screw is snugged down once the engine has been properly timed. This screw rests on the rubber grommet seal which holds the distributor in place in case the normal hold down device should loosen.

 

 

 

 

 

 After all of the work that I could do was finished, I boxed the engine case up and sent it over to Hummel Engines and had Scott Casler modify the case for his 92MM cylinder set up and a 78MM crank balance assembly.

 

 

 Like I mentioned earlier, I was going to try all of the machining my self but just don’t have the tools to do this type of work. Next time I will try the head conversion my self though. The heads that came off of the original engine are actually in pretty good shape. I think I will practice on them and if they come out I can use them as a spare set if needed in the future.

 

 While Scott Casler had the case, I ordered the crank, heads, bearings and a prop hub and had him ship it all back at the same time. I must add that Scott does an excellent job on the heads!!!

 

 

 

 

 

 

 

 

 

 

Next it was time to dry assemble the engine to make sure it all fit. I bought the .009 Bosch distributor and a VW seal kit from Mofoco down in Milwaukee, WI. The extra lobes on the distributor needed to be ground off to keep from sending extra unwanted sparks through out the distributor.       I made a drawing schematic of how I took the assembly apart so I could put it all back together again after the extra lobes were removed.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

I started the assembly by putting the distributor in first along with the required shims. I guess I won’t go into great detail of how I put the engine together but will say that I pretty much followed the “Great Plains aircraft Type 1 Engine Assembly Manual” to a tee. Between that and the other recommended “How to Rebuild Your Volkswagen Air Cooled Engine Manual”, the job went pretty smooth.

 

 

 

 I bought two 26MM Mikuni Carburetors from Central Snowmobile Salvage. Also purchased were two spigot mount rubber flanges, dual throttle cable and a choke cable assembly. I tried to find two 28MM carburetors but none were to be found. Used that is. The guy behind the counter who was also a mechanic said the 26MM carburetor has the same body that the 28MM carburetor uses and said that if the 26MM throat size was not effective I could take it to any reputable machine shop and have them drill the opening out to a 28MM size.

 

 

 After the engine was complete, I made a set of cooling tins to direct more air over the heads and cylinders out of cardboard, once satisfied with the shape I transferred them over to a sheet of .025 2024T3 aluminum and cut them out with a pair of tin snips. I finished them off with a smooth hand file.

 

 

  At this time, the engine has only one hour of run time, It runs great with the two 26MM carburetors. There were two small oil leaks that have since been fixed. I am getting approximately 3150 static RPM at this time. I’m told it should turn up a little more static so I guess I have a little more tuning to do.

 

 

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